Mitigating Condensate Recovery Problem for Boiler Feed Water in Wonji/ Shoa Sugar Factory

dc.contributor.advisorWondwossen, Bogale (PhD)
dc.contributor.authorHanfato, Haile
dc.date.accessioned2021-09-13T05:24:16Z
dc.date.accessioned2023-11-18T06:32:22Z
dc.date.available2021-09-13T05:24:16Z
dc.date.available2023-11-18T06:32:22Z
dc.date.issued2021-03
dc.description.abstractToday the competitiveness of sugar industry is dependent on the efficiency of the factory. The major contributor for the efficiency is the energy performance of the plant as sugar factory is one of intensive energy demanding manufacturing sector. Usually clarifications, evaporation, pan Boiling, and crystallization sections of sugar factory use most of thermal energy of the steam to concentrate and crystallize. In addition to run the factory without interruption continuous and sufficient supply of feed water is important. However, boilers of most sugar factories in Ethiopia are unable to supply enough steam for their respective factory operation purposes besides their electric power generation are not even self-sufficient rather they need external power supply to run the factory like Wonji shoa Sugar factory due to different reasons; one of the reasons is shortage of condensate to the Boiler as feed water. This is mainly known when exhaust steam supplied to first effect evaporator and clear juice heater is recovered only 87.5 % of it. 6.1 t/h or 146.4 tons per day hot Condensate is lost. That is 146.4 tons or 149,082 liters of treated heated water is required per day. Therefore, thermal energy performance of the factory can be improved by increasing the amount of condensate recovered and this is accomplished by avoiding intermittent crushing, reducing down times, crushing different cane varieties together, regular inspection and maintenance of leakages on steam-condensate lines and mainly manage exhaust steam temperature delivered to first effect evaporator and clear juice heater by controlling the amount of de-superheating water. Therefore, Boiler stoppage because of the drop of over flow level of hot well tank as the result of low condensate recovery will be reduced to zero. Consequently, the performance of the Boiler steam generation will be improved by 5%, and the loss of condensate will be minimized to zero so that avoiding downtime will help the factory to save about 7,400,000 birr per day and minimizing condensate loss helps the factory to save 4,621,543.4 birr per day. Totally the factory can save 12,021,543.4 birr per day.en_US
dc.identifier.urihttp://etd.aau.edu.et/handle/12345678/27855
dc.language.isoen_USen_US
dc.publisherAddis Ababa Universityen_US
dc.subjectCondensateen_US
dc.subjectBoileren_US
dc.subjectsteam trapen_US
dc.subjectexhaust steamen_US
dc.subjecthot well tanken_US
dc.subjectmake up wateren_US
dc.subjectevaporatoren_US
dc.subjectclear juice heateren_US
dc.titleMitigating Condensate Recovery Problem for Boiler Feed Water in Wonji/ Shoa Sugar Factoryen_US
dc.typeThesisen_US

Files

Original bundle
Now showing 1 - 1 of 1
No Thumbnail Available
Name:
Hanfato Haile.pdf
Size:
8.58 MB
Format:
Adobe Portable Document Format
License bundle
Now showing 1 - 1 of 1
No Thumbnail Available
Name:
license.txt
Size:
1.71 KB
Format:
Plain Text
Description: